{"id":782,"date":"2017-03-13T00:00:00","date_gmt":"2017-03-13T00:00:00","guid":{"rendered":"http:\/\/accuturn.spotlightdev.co.uk\/news\/process-improvements-machine-shop\/"},"modified":"2018-10-22T18:10:54","modified_gmt":"2018-10-22T17:10:54","slug":"process-improvements-machine-shop","status":"publish","type":"post","link":"https:\/\/accuturn.co.uk\/news\/process-improvements-machine-shop\/","title":{"rendered":"Process Improvements in the Machine Shop"},"content":{"rendered":"

With all the<\/strong> Lean improvements to the factory we’ve been making so far, it has left us in a great position to start having a look at our every day jobs and processes.  We can make improvements by recognising and then eliminating any waste<\/a> within every job we do.  Process improvements can allow us to<\/p>\n

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  1. make jobs easier and more enjoyable for staff<\/li>\n
  2. increase our efficiency<\/li>\n<\/ol>\n

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    What are some of the Process Improvements we’ve made at Stokes & Rowe?<\/h4>\n

    We are making process improvements every day.  Here are a few examples of some we have made in the machine shop this past week:-<\/p>\n

    \"ProcessWe used to have all our oils and lubricants stored in one central area.  We would decant it from a big tub into an oil can to transport to each machine.  There wasn’t enough clearance at the machine for the oil can, so we used a funnel in order to fill the tank.  This was a two person job, one holding the funnel, the other pouring.  It was clear that what should be a simple process had a lot of waste.  To improve this, we’ve abolished the oil store and now have a supply of oil next to each machine.  This instantly eliminates transport waste.  Each oil bottle also has it’s own oil can with flexible nozzle, so no more struggling with funnels and it’s a lot less messy!<\/p>\n

    We also found that undoing the tool holders on the machine turrets was a time consuming job.  This was previously done by hand with an alan key requiring a good deal of physical exertion.  This process took approximately one minute per tool holder.  A mere investment of \u00a340 on an air impact driver means that we can now remove all four bolts in eight seconds, with a lot less effort!  The saving of 52 seconds across 16 tool holders on a turret equates to a saving of approximately 14 minutes.  Using this same method to install the new tool holders for the next job gives us the same saving.  Over the two machines we are trialing this on, this adds up to a whole day per month in time saved.<\/p>\n